From: Quentin Schulz Date: Fri, 9 Feb 2024 13:18:09 +0000 (+0100) Subject: rockchip: ringneck-px30: put STM32_RST line in input mode instead of output X-Git-Url: http://git.dujemihanovic.xyz/?a=commitdiff_plain;h=73d72107919e93418f61cace088c1622fc25089b;p=u-boot.git rockchip: ringneck-px30: put STM32_RST line in input mode instead of output The STM32_RST line is routed to the ATtiny microcontroller PA0/RESET/UPDI pin. By driving the PX30 SoC pin as GPIO output high, we prevent external UPDI to be used for flashing without first putting this pin as GPIO input, an extra step we could avoid in userspace. There's an external hardware pull-up strong enough to keep the STM32_RST state high on ATtiny side but weak enough it can be overridden by external UPDI. This also means it is safe to use for the STM32 variant, where STM32_RST line will be in the same state as if output high was used. The Q7 standard specifies that MFG_NC1 and MFG_NC2 (used for UPDI for Ringneck) pins should neither be driven by the carrierboard, nor have pull-up or pull-down resistors. This means this commit is safe to use regardless of the carrierboard this module would be connected to (provided it follows the Q7 standard). Fixes: 6acdd63e8771 ("rockchip: ringneck-px30: always reset STM32 companion controller on boot") Cc: Quentin Schulz Signed-off-by: Quentin Schulz Reviewed-by: Kever Yang --- diff --git a/board/theobroma-systems/ringneck_px30/ringneck-px30.c b/board/theobroma-systems/ringneck_px30/ringneck-px30.c index bfebfe5136..c48de7345f 100644 --- a/board/theobroma-systems/ringneck_px30/ringneck-px30.c +++ b/board/theobroma-systems/ringneck_px30/ringneck-px30.c @@ -58,9 +58,9 @@ void spl_board_init(void) mdelay(1); - ret = gpio_direction_output(STM32_RST, 1); + ret = gpio_direction_input(STM32_RST); if (ret) { - debug("Failed to configure STM32_RST as output high\n"); + debug("Failed to configure STM32_RST as input\n"); return; } }